Demolition of original Tank FB-103 was executed due to the fact that the tank was in a significantly corroded state and it could not be used to storage of hydrocarbons. It was replaced by a new tank intended as a feed tank for primary naphtha to pyrolysis furnaces.
The aim of this project is to achieve the required quality of the produced stabilized gasoline from gasoline hydrogenation unit in sulfur and nitrogen content up 0.5 ppm throughout catalyst’s service life (60 months).
This job included ten projects aimed at improvement of the CCR unit reliability (reforming with continuous catalyst regeneration). Their execution was during the Litvínov refinery shutdown in 2016.
The aim of this project was a store tank replacement including a reconstruction of tank foundation with regard to environmental protection, naphtha piping modification in the pumping station and supply piping of the tank.
The aim of this project was an introduction of aviation kerosene production in JET-A1 quality at ČESKÁ RAFINÉRSKÁ, a.s. in refinery Litvínov. The subject of elaborated documentation was JET-A1 storage, filtration and expedition design.
The project addressed an expiring operational cycle of vibration sensors and axial shift sensors including an obsolete switchboard.
Installation of a dosing station and piping connection to an existing blender.
These projects allowed to operate the FCC unit without the VDU unit in the long term of operation. The project was executed during a shutdown of the refinery.
This project consisted of production and assembly of a new tank with a volume of 360 m3, which is a part of waste water treatment in ČESKÁ RAFINÉRSKÁ, a.s.
Design and installation of the process of automatic dewatering system for four gasoline storage tanks in Recope refinery in Costa Rica.